ملخص
A mechanism of a commingled Huff 'n Puff cycles of gas cross flow from a highly pressurized lower formation into a depleted upper formation has proven to be effective in reducing gas-well productivity losses due to near-wellbore condensate dropout. Compositional simulation was used to evaluate the performance of gas wells hampered by liquid dropout and to assess ways of producing the gas field. As a result of liquid re-vaporization the study shows that an appropriate scheduling of huff 'n puff shut-in and production cycles lead into a decline of in-situ liquid dropout and an increase in surface liquid recovery.
اللغة الأصلية | English |
---|---|
الصفحات (من إلى) | 517-533 |
عدد الصفحات | 17 |
دورية | Petroleum Science and Technology |
مستوى الصوت | 25 |
رقم الإصدار | 4 |
المعرِّفات الرقمية للأشياء | |
حالة النشر | Published - أبريل 2007 |
ASJC Scopus subject areas
- ???subjectarea.asjc.1600???
- ???subjectarea.asjc.1500???
- ???subjectarea.asjc.2100.2103???
- ???subjectarea.asjc.2100.2102???
- ???subjectarea.asjc.1900.1909???